So.... I installed the .22 mod utilizing two #4 washers. I also opened up the fuel screw to 1 3/4 turns. Took the bike out and discovered it was running horribly rich at the low end. So, I removed one of the washers. Took another test ride and found the bike better but still running horribly rich at the low end. I am now scratching my head.... I reset the fuel screw to a tad over one turn took another test ride. Still... horribly rich at low end. I remove the remaining washer, essentially putting the needle to stock position. Start it up and find it is still running horribly rich at the low end. I readjust the fuel screw to exactly one turn out. I also notice the overflow hose on the carb had been melted. apparently, it touched a pipe sometime in the PO's life. I made a quick repair and started the bike up. Hmmmm.... doesn't seem to be loading up on low end anymore. I look under the bike and crap! The bike is leaking fuel big time. I just it down and turn off the petcock. As I am cleaning up the spilt fuel, I see the piece of burned hose I had cut off. I noticed that it had been burned shut. In essence, it was sealed and clearly wouldn't allow fuel to pass through it. I then realized I may have a float issue. The float might not be shutting off the fuel. The overflow wasn't draining it because it had been sealed. I pull the carb (Majot PITA BTW) and remove the bowl. Everything looks ok so far. needle is moving in conjunction with the float ok. I check float height, it's ok as well. I blow into the fuel line with the float in the shut off position. I can still move air. I then remove the float and needle and take a look inside the seat. Lo and behold! There is something in there. I remove it and see it is a metal burr of some sort and it was preventing the needle from seating properly. It was constantly dumping fuel into the engine. If it sat idling, it would load up and stall. I cannot imagine how that got in there. I cleaned it out and put the carb back together and reinstalled it on the bike. (another major PITA lol). Put the tank on again (for the 50th time) and reconnected all lines and fired her up. She sat there ticking over perfectly. No more loading up. By this time, it was too late to take her out for a test drive. I will do that tomorrow. What an experience. All that work and I am right back where I started. I did get a chance to see what effect the washers have on performance. My issues were only low end not midrange or above. I did remove the flat spot with just one washer and it seemed to run ok but, it felt like it lost a little power. I will run it without the mod for a while. If I decide to install a 685 Kit, I will set it up properly with the KLX kit. BTW, the fuel screw is currently sitting at 1 1/2 turns out. I am expecting (hoping) the test ride tomorrow will be pretty much like it was before I started this little project.